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| NTSB Identification: LAX99LA314. The docket is stored in the (offline) NTSB Imaging System. |
| Accident occurred Monday, September 20, 1999 at BIG BEAR CITY, CA |
| Aircraft: Cessna 177A, registration: N39AE |
| Injuries: 1 Uninjured |
| Event: 20001212X19813 Status: Final Report Approved On Friday, April 06, 2001 |
| NTSB Preliminary Narrative (6120.19A) |
| On September 20, 1999, about 1139 hours Pacific daylight time, a Cessna 177A, N39AE, ditched in Big Bear Lake after losing power near Big |
| Bear City, California. The aircraft sustained substantial damage; however, the certificated airline transport pilot, the sole occupant, was not |
| injured. The aircraft was being operated under the provisions of 14 CFR Part 91 by the pilot as a maintenance test flight when the accident |
| occurred. The flight originated from the Big Bear City Airport about 1130. Visual meteorological conditions prevailed at the time and no flight plan |
| was filed. |
| The pilot reported that the aircraft had been parked outside, on the ramp, for nearly 7 months. The owner had reported that the left main tank |
| had been "seeping." At the time the aircraft was parked, both fuel drains were removed and all fuel was drained from the tanks. At the end of |
| the period of inactivity, an airframe and powerplant mechanic (A&P) replaced the fuel drain in the aircraft's right tank and added fuel to prepare |
| the aircraft for a ferry flight to Corona, California. After sitting for most of a day, no leaks were noted. The mechanic then added enough |
| additional fuel to bring the level up to 20 gallons. The pilot performed a preflight and before takeoff checks; however, the engine stalled once |
| during taxi. |
| On the first flight, the pilot had climbed to 8,000 feet msl when he found that the engine began to miss and run roughly. After returning, the pilot |
| again drained the fuel sumps and obtained a "small amount of water" from the gascolator. He then drained an additional gallon of fuel from the |
| tank, and at that time, did not find any additional water or sediment. The pilot's procedures were observed by the mechanic. |
| Prior to takeoff on the accident flight, the pilot again performed the same preflight and before takeoff checks. This time the checks were |
| performed without incident. The mechanic did not perform or offer to perform any additional troubleshooting procedures between the first and |
| second flight. |
| The pilot reported that he took off with about 18 gallons of fuel in the right main tank. After takeoff, he climbed to 7,500 feet msl heading east of |
| the airport and over the lake. After reaching 7,500 feet, the engine began surging and then quit. He turned on the electric fuel boost pump, |
| pushed the mixture handle into the "full rich" position, and "pumped" the throttle. When his attempts to restart the engine failed, he turned back |
| toward the airport but was unable to reach the runway. He ditched the airplane in about 1.5 feet of water, 50 yards from the south shore of the |
| lake, west of the Stanfield cutoff. After touching down, the aircraft nosed over and came to rest on its back. The pilot turned off the electric |
| fuel pump and master switch, and crawled out of the cockpit and onto the wing. He waited there until rescued by boaters who had witnessed |
| the accident. |
| On November 1, 1999, a Safety Board investigator examined the engine and airframe at Action Towing and Recovery in Fresno, California. A |
| cold compression check of the Nos. 1 through 4 cylinders revealed the following readings: 62, 61, 61, and 63 psi, respectively. All four top |
| spark plugs were removed and examined. The tips of all four plugs were covered with a similar looking brownish substance consistent with the |
| color and texture of rusted metal. |
| The inside of the gascolator was found to be coated with an apparently insoluble greenish-brown film. The left wing fuel quantity transmitter |
| was removed and examined. It was coated with material that was similar in appearance to silicon sealant. The material was decomposing and |
| readily flaked off when touched. The fuel reservoir drain plug was removed and approximately 10cc of liquid was recovered. The liquid |
| precipitated into a lower layer and upper layer in a manner similar to the precipitation that follows the mixture of water and gasoline. The sample |
| also contained some heavier sediment that was similar in color and consistency as to the sealant-like material found on the fuel quantity |
| transmitter. |
| The above noted discrepancies were located in areas that are not accessible or serviceable by a pilot performing a preflight inspection or before |
| takeoff checks. |
| NTSB Final Narrative (6120.4) |
| The aircraft was parked outside on the ramp for several months, with the fuel drains removed and the tanks drained. An A&P mechanic |
| replaced the fuel drain in the right tank and added fuel for a maintenance ferry flight. The pilot performed a preflight and before takeoff checks. |
| The engine stalled once during taxi, then began to miss and run roughly after takeoff. After returning, the pilot drained the fuel sumps and found |
| a 'small amount of water' in the gascolator. He then drained an additional gallon of fuel from the tank without finding any additional water or |
| sediment. After takeoff on the second flight, the engine began surging and then quit. When attempts to restart the engine failed, he turned back |
| toward the airport but could not reach the runway and ditched the airplane in the water. The mechanic did not perform or offer to perform any |
| additional troubleshooting procedures between the first and second flight. The inside of the gascolator was coated with an insoluble |
| greenish-brown film. The left wing fuel quantity transmitter was coated with material that was similar in appearance to a non-silicon sealant. |
| The material was decomposing and readily flaked off when touched. About 10cc of liquid was recovered from the fuel reservoir; about half |
| was water, with a heavier sediment that was similar in color and consistency as to the material coating the fuel quantity transmitter. The above |
| noted discrepancies were located in areas that would not be accessible or serviceable by a pilot performing a preflight inspection. |
| NTSB Probable Cause Narrative |
| A loss of engine power due to fuel system contamination, which resulted from the mechanic's failure to fully inspect and verify the serviceability |
| Occurrences and Sequence of Events |
| Occurrence: 1, LOSS OF ENGINE POWER(TOTAL) - MECH FAILURE/MALFUNCTION |
| Phase of Operation: TAKEOFF - INITIAL CLIMB |
| Sequence of Events for Occurrence Number: 1 |
| 1 ( Cause ) FUEL SYSTEM / CONTAMINATION, OTHER THAN WATER / (0) |
| 2 ( Cause ) MAINTENANCE, INSPECTION / INADEQUATE / OTHER MAINTENANCE PERSONNEL |
| 3 ( Factor ) OPERATION WITH KNOWN DEFICIENCIES IN EQUIPMENT / ATTEMPTED / PILOT IN COMMAND |
| Occurrence: 2, FORCED LANDING |
| Phase of Operation: EMERGENCY DESCENT/LANDING |
| Sequence of Events for Occurrence Number: 2 |
| 4 (Finding) TERRAIN CONDITIONS / WATER / (0) |
| Occurrence: 3, DITCHING |
| Phase of Operation: EMERGENCY LANDING AFTER TAKEOFF |
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