Home Documents Images Message Board
(Use your browser's back button to return to the page that you were previously viewing.)
| NTSB Identification: LAX99LA267. The docket is stored in the (offline) NTSB Imaging System. |
| Accident occurred Wednesday, August 11, 1999 at AGANA, OF |
| Aircraft: Cessna 152, registration: N64813 |
| Injuries: 1 Fatal |
| Event: 20001212X19555 Status: Factual |
| NTSB Preliminary Narrative (6120.19A) |
| HISTORY OF FLIGHT |
| On August 11, 1999, at 1439 hours local island time, a Cessna 152, N64813, was destroyed when it impacted terrain during an emergency |
| landing following loss of engine power near Agana, Guam. The commercial pilot, the sole occupant, was fatally injured. The local area flight |
| was operated by the pilot under the provisions of 14 CFR Part 91. Visual meteorological conditions prevailed and no flight plan was filed for the |
| personal flight, which departed from Guam International Airport at 1419. |
| According to a witness, the aircraft performed a low pass from west to east over the closed Windward Hills Airport at 150 feet agl. After flying |
| over the 2,000-foot-long grass runway, the aircraft performed a pull-up maneuver during which the engine lost power. The aircraft performed a |
| steep turn maneuver to the right during which the engine recovered power, and then lost power a second time. The aircraft turned |
| approximately 90 degrees to the right during the pull-up maneuver and engine power interruption. The aircraft was next observed to reverse the |
| direction to the left and turned about 270 degrees to realign with the runway. While aligning with the runway, the left wing tip struck terrain, the |
| aircraft cart wheeled, and there was an ensuing postcrash fire, which consumed the majority of the wreckage. |
| PERSONNEL INFORMATION |
| The pilot's logbook was not located after the accident. On the pilot's application for his airman's medical certificate, dated January 26, 1999, the |
| pilot reported having 4,000 hours total time with 150 hours in the previous 6 months. |
| AIRCRAFT INFORMATION |
| The aircraft was modified in accordance with Supplemental Type Certificate (STC) SA2613CE (ROC Aviation, Taipei, Taiwan, ROC) on June 26, |
| 1997. The STC authorizes operation of the aircraft using automotive gasoline. According to the pilot's partner in ownership of the aircraft, the |
| aircraft was fueled with aviation fuel (avgas) at the time of the accident. |
| An annual inspection was performed on July 16, 1999. |
| WRECKAGE AND IMPACT INFORMATION |
| Because of the distant location, the Safety Board investigator did not travel to the accident location. The engine from the aircraft was shipped to |
| the mainland and was examined by the Safety Board at the facilities of Aircraft Recovery Service in Compton, California, on October 13, 1999. |
| The engine had impact and fire related damage. The propeller flange was bent aft about 10 degrees over a sector angle of about 45 degrees |
| and the alternator and associated brackets were bent aft about 1 inch. The muffler exhaust pipe was collapsed at the outlet end and there was |
| dried mud in the muffler. The shape of the mud conformed to the collapsed outlet. The inlet air filter and carburetor heat box were intact but |
| partially collapsed. |
| The carburetor heat box was obstructed at the alternate air entry with dried mud and grass. The top of the engine and the upper portion of the |
| accessory case exhibited heat damage. The upper spark plug wires were heat damaged and the magnetos and vacuum pump exhibited heat |
| signatures. The engine was rotated and exhibited mechanical continuity, valve function, and accessory rotation. |
| The foam-type carburetor air filter was intact, the carburetor heat valve was in the midrange position and the throttle was in the full throttle |
| position. The carburetor base was cracked adjacent to one mount hole. |
| The exhaust muffler was clear internally with no flame tubes evident. The exhaust manifold tubes were internally dark gray/black where they |
| attach to the engine exhaust ports and no wet oil was found. |
| The vacuum pump and shear coupling, the starter motor, and the alternator were intact and externally undamaged. They were not internally |
| examined. |
| The spark plug electrodes were clean and dark gray in color. The electrodes were round and exhibited minimal wear. Both magnetos were |
| externally heat damaged and the ignition points did not function. The impulse coupling on the left magneto audibly snapped at top dead center |
| with number one cylinder on compression stroke. The left magneto had an impact mark on the tower cap and a 1/4 by 2-inch section of the |
| mounting base flange was broken. |
| The engine sump was removed and was free of debris. The oil suction screen was also free of debris. The accessory case was removed |
| and the accessory gearing was visibly undamaged. The crankshaft gear dowel pin was intact. |
| The 4 cylinder assemblies and pistons were removed and the internal bores were clean and shiny. The combustion chambers and piston faces |
| had moderate carbon deposits. The piston rings were intact. |
| The crankcase was separated. The crankcase bearings exhibited a uniform dull gray appearance and the journals of the crankshaft were |
| bright, shiny, and not scored. The camshaft was undamaged and the lobes did not exhibit wear. The no. 1 exhaust follower exhibited minor |
| spalling but no exfoliation. The remaining followers were shiny and unremarkable. |
| The carburetor was further examined by the Safety Board at the facilities of Precision Airmotive Corporation in Everett, Washington on October |
| 28, 1999. When placed on a flow bench it was noted that the float was stuck in one position, and it was necessary to tap the carburetor to free |
| the float after which the carburetor flow tested satisfactorily. The fuel inlet screen was clear. When disassembled, the float bowl chamber |
| was found to be contaminated with sand and was corroded. The metering nozzle was difficult to remove due to corrosion and the idle tube |
| was seized and could not be removed. |
| MEDICAL AND PATHOLOGICAL INFORMATION |
| An autopsy was performed by the Office of the Chief Medical Examiner in Tamuning, Guam, file number ME-101-99. A toxicology analysis was |
| performed by the FAA Civil Aeromedical Institute in Oklahoma City, Oklahoma. |
| ADDITIONAL INFORMATION |
| The aircraft's engine was released to Mr. Victor Reyes, the pilot's partner in ownership, on December 28, 1999. |
| Occurrences and Sequence of Events |
| No Occurrence records were found for: |
| NTSB Identification: LAX99LA267 |
| Event ID: 20001212X19555 |
| Aircraft Key: 1 |
Home Documents Images Message Board
(Use your browser's back button to return to the page that you were previously viewing.)