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| NTSB Identification: FTW98LA210. The docket is stored in the (offline) NTSB Imaging System. |
| Accident occurred Sunday, May 10, 1998 at STILLWATER, OK |
| Aircraft: Cessna 152, registration: N67326 |
| Injuries: 2 Minor |
| Event: 20001211X10064 Status: Final Report Approved On Tuesday, December 08, 1998 |
| NTSB Preliminary Narrative (6120.19A) |
| On May 10, 1998, at 1830 central daylight time, a Cessna 152 airplane, N67326, was substantially damaged during a forced landing following |
| the loss of engine power near Stillwater, Oklahoma. The private pilot and his passenger sustained minor injuries. The airplane was owned and |
| operated by Crabtree Aviation Inc., of Guthrie, Oklahoma, under Title 14 CFR Part 91. Visual meteorological conditions prevailed for the personal |
| flight for which a flight plan was not filed. The flight, which was destined for the Guthrie Municipal Airport, was originating at the time of the |
| accident. |
| The pilot reported to law enforcement personnel that responded to the accident, that he planned a normal departure from runway 17 at the |
| Stillwater Municipal Airport. The 189 hour pilot reported that while over the departure end of the runway, at an estimated altitude of 60 to 80 feet |
| above the ground, the engine started to run rough and then lost power. The pilot added that he lowered the nose of the airplane and made a |
| turn to the left for an emergency landing in a field adjacent to the airport. |
| The pilot reported that that the airplane touched down hard in a level attitude within the airport boundary, approximately 25 to 30 feet short of the |
| airport perimeter fence. The airplane rolled on the ground for 2 or 3 seconds prior to going through a barbed wire fence, impacting a ditch with |
| the nose wheel, and the nosed over. The airplane came to rest in the inverted position on a westerly heading on the north bound lane of the |
| Airport Industrial Access Road, approximately a mile south of the departure end of runway 17. |
| The pilot was issued his private pilot certificate on March 6, 1998. Law enforcement personnel requested a blood sample from the pilot for |
| alcohol testing. The pilot voluntarily agreed to submit himself for the blood alcohol test. Toxicological tests were negative for alcohol. |
| Examination of the wreckage by the FAA inspector confirmed that the forward section of the fuselage sustained structural damage. Examination |
| of the fuel system revealed that water was present in the fuel gascolator, as well as in the right wing fuel cell. The fluid drained from the |
| airplane was tested by an independent laboratory. The fluid was determined to be "drinking water." |
| In the narrative portion of the enclosed NTSB Form 6120.1/2, the pilot stated that he was very familiar with the preflight inspection of the airplane, |
| having accumulated nearly 60 hours in the type and model of airplane. He added that he performed a detailed preflight prior to his departure |
| from Guthrie, and no contaminants were found on either wing tank. The pilot stated that he found a "small bubble" of water when he drained the |
| gascolator during the preflight, but no evidence of additional water was detected after he drained additional fuel. |
| NTSB Final Narrative (6120.4) |
| The engine lost power during initial takeoff climb while at an estimated altitude of 60 to 80 feet above the ground. The pilot lowered the nose and |
| made a slight turn to the left in an attempt to make an emergency landing in a field adjacent to the airport. The airplane touched down hard in a |
| level attitude within the airport property, approximately 25 to 30 feet short of the airport perimeter fence. The airplane rolled on the ground for 2 |
| or 3 seconds prior to going through a barbed wire fence, impacted a ditch with the nose wheel, and the nosed over. Examination of the fuel |
| system revealed that water was present in the fuel gascolator, as well as in the right wing fuel cell. The fluid drained from the airplane was |
| tested by an independent laboratory. The laboratory confirmed that the fluid was 'drinking water.' |
| NTSB Probable Cause Narrative |
| The loss of engine power due to water contamination of the fuel. A factor was the lack of suitable terrain available for the forced landing. |
| Occurrences and Sequence of Events |
| Occurrence: 1, LOSS OF ENGINE POWER |
| Phase of Operation: TAKEOFF - INITIAL CLIMB |
| Sequence of Events for Occurrence Number: 1 |
| 1 ( Cause ) FLUID, FUEL / CONTAMINATION, WATER / (0) |
| 2 (Finding) AIRCRAFT PREFLIGHT / INADEQUATE / PILOT IN COMMAND |
| Occurrence: 2, FORCED LANDING |
| Phase of Operation: EMERGENCY LANDING AFTER TAKEOFF |
| Occurrence: 3, NOSE OVER |
| Phase of Operation: EMERGENCY LANDING AFTER TAKEOFF |
| Sequence of Events for Occurrence Number: 3 |
| 1 ( Factor ) TERRAIN CONDITIONS / NONE SUITABLE / (0) |
| 2 (Finding) TERRAIN CONDITIONS / DITCH / (0) |
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