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| NTSB Identification: ANC99LA096. The docket is stored in the (offline) NTSB Imaging System. |
| Accident occurred Thursday, July 22, 1999 at KODIAK, AK |
| Aircraft: Cessna 185, registration: N4949E |
| Injuries: 1 Minor |
| Event: 20001212X19139 Status: Final Report Approved On Monday, December 04, 2000 |
| NTSB Preliminary Narrative (6120.19A) |
| On July 22, 1999, at 1225 Alaska daylight time, a float equipped Cessna 185 airplane, N4949E, sustained substantial damage during an off |
| airport forced landing in a rocky riverbed, about eight miles west of the Kodiak Airport, Kodiak, Alaska. The solo commercial pilot received minor |
| injuries. The airplane was operated by the pilot under 14 CFR Part 91 as a business flight from the Lily Lake Seaplane Base in Kodiak, to the |
| Uganik Cannery on Kodiak. Visual meteorological conditions prevailed at the time of the accident, and a company VFR flight plan was filed. |
| The pilot told the NTSB investigator-in-charge (IIC) during a telephone interview on July 22, that the airplane was in cruise over mountainous |
| terrain, about 1,600 feet above sea level, when the fuel pressure dropped. The pilot said he switched fuel tanks, ensured the mixture control |
| was full forward, and turned on the electric fuel boost pump, but the engine did not restart. The pilot transmitted to a helicopter in the area that |
| he was making an emergency landing. During the landing, the airplane nosed over. |
| The pilot of the helicopter told the IIC during a telephone interview on July 22, that after the airplane came to rest, he landed to assist the |
| accident pilot. The helicopter pilot noted that he turned the magneto switch to OFF, and turned off both sides of the battery/alternator switch. He |
| smelled fuel, and saw fuel dripping from both wings. |
| On August 18, the IIC and an FAA inspector operated the engine while it was installed on the airplane. The engine started, operated normally, |
| and accelerated to full power. The electric fuel boost pump operated normally in both the HIGH and LOW boost position. The exhaust muffler |
| was internally inspected, and no blockages were found. No anomalies were noted with the engine. |
| The Cessna 185 Service Manual fuel system troubleshooting procedures (pages 13-3 and 13-4) were followed by the NTSB IIC and the FAA |
| inspector. No anomalies were noted. The fuel header tank shutoff valve operated fully and freely. All screens and filters were inspected and |
| found to be unobstructed. All flexible fuel lines were removed, cut open, and inspected at the NTSB Materials Laboratory on October 13, 1999, |
| with no blockages noted. On February 28, 2000, the electric fuel boost pump, and the free flow bypass valve, were tested at the |
| manufacturer's facility under the supervision of an NTSB investigator, with no anomalies discovered. |
| NTSB Final Narrative (6120.4) |
| The airplane was in cruise flight when all engine power was lost. The pilot switched fuel tanks, and activated the electric fuel boost pump. The |
| engine did not restart, the airplane landed in a rocky riverbed, and nosed over. A witness stated that fuel was leaking from both wings at the |
| accident site, and the magnetos and electric fuel boost pump switches were in the ON position. The NTSB investigator-in-charge and an FAA |
| airworthiness inspector operated the engine on the airplane, with no anomalies noted. All flexible fuel lines were removed and internally |
| inspected, the electric fuel pump and bypass valve were removed and tested, and all IO-520 maintenance manual troubleshooting procedures |
| were followed by the IIC and FAA inspector, with no anomalies noted. |
| NTSB Probable Cause Narrative |
| The total loss of engine power for undetermined reasons. A factor in this accident was the mountainous terrain in which the pilot had to perform |
| a forced landing. |
| Occurrences and Sequence of Events |
| Occurrence: 1, LOSS OF ENGINE POWER |
| Phase of Operation: CRUISE |
| Sequence of Events for Occurrence Number: 1 |
| 1 ( Cause ) REASON FOR OCCURRENCE UNDETERMINED / / |
| Occurrence: 2, ON GROUND/WATER ENCOUNTER WITH TERRAIN/WATER |
| Phase of Operation: EMERGENCY DESCENT/LANDING |
| Sequence of Events for Occurrence Number: 2 |
| 1 ( Factor ) TERRAIN CONDITIONS / MOUNTAINOUS/HILLY / (0) |
| Occurrence: 3, NOSE OVER |
| Phase of Operation: EMERGENCY DESCENT/LANDING |
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