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| NTSB Identification: ANC99LA052. The docket is stored in the (offline) NTSB Imaging System. |
| Accident occurred Tuesday, April 27, 1999 at JUNEAU, AK |
| Aircraft: Cessna 185, registration: N93311 |
| Injuries: 1 Serious, 1 Minor |
| Event: 20001205X00410 Status: Final Report Approved On Friday, June 23, 2000 |
| NTSB Preliminary Narrative (6120.19A) |
| On April 27, 1999, at 1409 Alaska daylight time, an amphibious float equipped, Cessna 185 airplane, N93311, sustained substantial damage |
| when it landed short of runway 26 at the Juneau International Airport, Juneau, Alaska. The commercial pilot received minor injuries. The |
| passenger received serious injuries. The flight was operated under 14 CFR Part 135 as an on-demand air taxi by Ward Air, Inc., of Juneau. The |
| flight departed Hawk Inlet, Alaska, for Juneau at 1359. Visual meteorological conditions prevailed at the time of the accident, and a company |
| VFR flight plan was on file. |
| The pilot told two FAA inspectors at the scene that the engine suddenly quit when the airplane was 300 feet above the ground, during final |
| approach to land. The pilot indicated that he turned on the electric fuel pump, but the engine did not restart. He also stated he retracted the flaps |
| to attempt to increase the glide distance. The airplane landed in soft mud short of the runway, and nosed over. The pilot said that both |
| occupants were wearing shoulder harnesses at the time of the accident. The pilot repeated these statements to the NTSB |
| investigator-in-charge (IIC) during a telephone interview on April 28. |
| The passenger stated to the IIC he was not wearing a shoulder harness, and was not aware that there was one. |
| Initial inspection of the airplane by FAA inspectors revealed that the engine crankshaft was intact, and fuel was present in both wing tanks. The |
| flaps were extended to 30 degrees, the landing gear handle was down, and the wheels were extended. The FAA inspectors applied power to |
| the electric boost pump and confirmed that it operated normally. No other mechanical anomalies were noted with the engine. |
| The engine driven fuel pump, Continental Motors (TCM) part number 64905A6R, was flow tested on a test bench under the direction of the NTSB |
| IIC on May 3, 1999. The pump repeatedly would not maintain a prime, had air drawn into the system, and would not pump fuel. Disassembly of |
| the pump did not reveal any visible passage or orifice blockages, nor torn gaskets or seals. A telephone conversation by the NTSB IIC with the |
| TCM chief accident investigator on June 15 revealed that the likely source of air into the pump was either the forward fuel seal, or a blocked |
| vapor tower jet. |
| Additionally, the Emergency Locator Transmitter (ELT), Sharc-7 model # 7J4-193, did not operate during the accident. Inspection of the ELT at |
| the NTSB laboratory on June 10 revealed that the ELT was installed in the airplane in November 1998. The installed battery pack was |
| manufactured in February 1999, and installed into the ELT on an unknown date between February 1999 and April 27, 1999. One of the internal |
| battery terminal connectors was found fractured, and disconnected. Microscopic examination at the NTSB materials laboratory revealed tool |
| markings on the connector consistent with those left by pliers. Installation of the adjacent battery required bending the connector and wire out |
| of the way. |
| NTSB Final Narrative (6120.4) |
| The amphibious airplane was about 300 feet above the ground, on short final to land on the runway, when the engine quit. The airplane landed |
| in soft mud with the wheels extended, and flipped over. Postaccident examination revealed fuel in both wing tanks. Bench testing revealed the |
| engine driven fuel pump would not pump fuel, and drew air into the pump when primed and operated. Disassembly did not reveal any |
| blockages, damaged seals, or sources of the air leak. |
| NTSB Probable Cause Narrative |
| The failure of the engine driven fuel pump for undetermined reasons. Factors associated with this accident were the low altitude at which the |
| failure occurred resulting in task overload of the pilot, and landing the amphibious airplane in the swampy terrain short of the runway with the |
| Occurrences and Sequence of Events |
| Occurrence: 1, LOSS OF ENGINE POWER(TOTAL) - MECH FAILURE/MALFUNCTION |
| Phase of Operation: APPROACH - VFR PATTERN - FINAL APPROACH |
| Sequence of Events for Occurrence Number: 1 |
| 1 ( Cause ) FUEL SYSTEM, PUMP / INOPERATIVE / (0) |
| 2 (Finding) REASON FOR OCCURRENCE UNDETERMINED / / |
| Occurrence: 2, NOSE OVER |
| Phase of Operation: EMERGENCY DESCENT/LANDING |
| Sequence of Events for Occurrence Number: 2 |
| 1 ( Factor ) TERRAIN CONDITIONS / SWAMPY / (0) |
| 2 ( Factor ) ALTITUDE / LOW / |
| 3 ( Factor ) EXCESSIVE WORKLOAD (TASK OVERLOAD) / (0) / PILOT IN COMMAND |
| 4 ( Factor ) WHEELS DOWN LANDING IN WATER / PERFORMED / PILOT IN COMMAND |
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